RE: Motor Gone
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RE: Motor Gone - 5/5/2008 3:20:50 PM
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sawyer
Posts: 642
Joined: 11/19/2006 Status: offline
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quote:
ORIGINAL: Simon1 quote:
ORIGINAL: tached_out Adam doesnt do my wrenching but he does all of my tuning. I can also vouch for that he does a great job tuning my car. He got me 550rwhp with no tuning only drivability at 5,000rpms on 9 psi and we plan to see any thing from 15-17psi once we are finished at max rpms. The car drives like it is stock and I dont think I would have any one else tune my car other then him. My turbo maxes out at 16 psi, I could upgrade it but probably won't right now. I've been shopping around at DSS and MMR and I'm leaning toward an iron block, stroked to 298 ci with all the "small" things added in to make it stronger, more durable. I'm gonna try and get the car up in the air today to take some pictures of the carnage. Hey Clint, I was talking to Adam about the lose ends on my build and I told him about your motor. I PM'd you his email address, he can get you in next week or the week after At least call Adam, he has a minimum of 8 10 second daily drivers out there( and a ton of other built motors) with ZERO engine failures that I know of. All his builds are done in house for quality control.
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Whipple 3.4, 4R70W Built and Tuned by ST Motorsports 636 RWHP 594TQ http://www.modernmustangmuscle.com/tech/whipplemustanggt.html
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RE: Motor Gone - 5/5/2008 3:35:29 PM
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kolb02
Posts: 150
Joined: 5/6/2007 Status: offline
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Sorry to here about the motor I totally know how you feel, I'll post pics of my short block tonight when I get it out of the car.
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Saleen Blower,Brenspeed stage 4, 4:10's, BBK O/R X, Borla Exhuast, BMR springs, BMR LCA's, Aluminum DS, Brenspeed Heat exchanger
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RE: Motor Gone (pics) - 5/5/2008 4:12:21 PM
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moosestang
Posts: 7097
Joined: 9/3/2006 From: Gainesville, FL Status: online
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quote:
ORIGINAL: sactown Hey Simon1, I am working Saturday morning, but I can give you hand with the car after that if you need one. But damn that is horrible. I hope my sh!t does not go boom when I try to reload the new tune tomorrow. Sactown Don't do it! These things tend to come in 3's! OH wait, that's people dying. But that is 2 motors in 2 weeks, so.........
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whipple HO SC,FRPP springs, Pypes mid mufflers, Che adj. LCA, hurst, 4.10's, 1 piece DS, spec stg 2 clutch. Accel coils 12.52@117.6mph so far with a 2.01 60 ft time(pre shaft, coils, clutch).
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RE: Motor Gone - 5/5/2008 4:15:39 PM
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onederful100
Posts: 2281
Joined: 7/11/2007 From: parts unknown Status: offline
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quote:
ORIGINAL: moosestang quote:
ORIGINAL: ShelbyDoc My motor let go at 3200 rpm's normal light throttle at 30mph. Two rods one through the side and one through the top! http://s73.photobucket.com/albums/i214/flalv/doc/?action=view¤t=kaboom008.jpg What was your setup, power level, psi? I know it wasn't a twinscrew just by looking at the above pic. he's got a procharger. i checked hammeron's FI guest book and he signed in 2/12/2008, 2 days before i did.
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2007 GT 5spd Whipple Crew Member Boomtube Crew Member My Car
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RE: Motor Gone - 5/5/2008 4:33:17 PM
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ShelbyDoc
Posts: 38
Joined: 12/27/2007 Status: offline
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The pics were after motor pulled. Procharger at 6psi professionally tuned. Boost was going out the bypass at the time. I was not even on the throttle much. Had just turned out of my subdivision. New motor in this week.
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RE: Motor Gone - 5/5/2008 4:41:09 PM
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blueherd02gt
Posts: 3971
Joined: 5/26/2006 From: Tennessee Status: offline
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I know what you mean. I honestly would put 10k in a motor build and do it right. Honestly I'd get a 298cu/in stroker motor and be done with it. It sounds like ST needs to hire some wrenches and expand. They ,miight be loosing customers with their waiting list... quote:
ORIGINAL: Simon1 quote:
ORIGINAL: blueherd02gt Damn.... Budget? Budget? What's that mean? I really don't know. I don't like to toot my own horn, but I have the money to run side by side with Modaddict, but I choose to not do it. I am very , how shall I say, frugal? with my money. Cheap things cost too much, so I buy the expensive ones that last forever. I am married with little kids so I need to save some for later. LOL
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Whipple Crew Member 468whp 463 lb/ft tq 2007 Black premium GT BMC member #07208
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RE: Motor Gone - 5/5/2008 4:42:16 PM
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onederful100
Posts: 2281
Joined: 7/11/2007 From: parts unknown Status: offline
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doesnt sound like too much boost at all, i wonder what made it blow like that. what was your a/f like?
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2007 GT 5spd Whipple Crew Member Boomtube Crew Member My Car
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RE: Motor Gone - 5/5/2008 4:45:08 PM
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hammeron
Posts: 7785
Joined: 5/17/2006 Status: offline
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it's turned into a historical archive cough *stickey* cough quote:
ORIGINAL: onederful100 he's got a procharger. i checked hammeron's FI guest book and he signed in 2/12/2008, 2 days before i did.
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RE: Motor Gone - 5/5/2008 5:10:20 PM
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onederful100
Posts: 2281
Joined: 7/11/2007 From: parts unknown Status: offline
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quote:
ORIGINAL: hammeron it's turned into a historical archive cough *stickey* cough quote:
ORIGINAL: onederful100 he's got a procharger. i checked hammeron's FI guest book and he signed in 2/12/2008, 2 days before i did. +1 on the sticky! just a little mustangforum private investigating. and when i looked i was the last person to sign it too. and i just might sign it again!
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2007 GT 5spd Whipple Crew Member Boomtube Crew Member My Car
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RE: Motor Gone - 5/5/2008 5:22:03 PM
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moosestang
Posts: 7097
Joined: 9/3/2006 From: Gainesville, FL Status: online
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quote:
ORIGINAL: ShelbyDoc The pics were after motor pulled. Procharger at 6psi professionally tuned. Boost was going out the bypass at the time. I was not even on the throttle much. Had just turned out of my subdivision. New motor in this week. I could tell it wasn't a twinscrew because of the knock sensor wires and the stock coolant tube running down the engine valley. Why do you think the motor let go with no boost? That doesn't seem normal, unless something allready cracked or bent on your last jaunt. What were your dyno numbers? You might want to find a new professional.
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whipple HO SC,FRPP springs, Pypes mid mufflers, Che adj. LCA, hurst, 4.10's, 1 piece DS, spec stg 2 clutch. Accel coils 12.52@117.6mph so far with a 2.01 60 ft time(pre shaft, coils, clutch).
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RE: Motor Gone - 5/5/2008 5:42:00 PM
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moosestang
Posts: 7097
Joined: 9/3/2006 From: Gainesville, FL Status: online
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quote:
ORIGINAL: blueherd02gt I know what you mean. I honestly would put 10k in a motor build and do it right. Honestly I'd get a 298cu/in stroker motor and be done with it. It sounds like ST needs to hire some wrenches and expand. They ,miight be loosing customers with their waiting list... I have more respect for a shop that would turn me away because they have to much on their plate, than one that would string me along because they don't want to lose any business. That's what happened with my gears and I found a shop that needed the business. The other shop lost my business forever.
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whipple HO SC,FRPP springs, Pypes mid mufflers, Che adj. LCA, hurst, 4.10's, 1 piece DS, spec stg 2 clutch. Accel coils 12.52@117.6mph so far with a 2.01 60 ft time(pre shaft, coils, clutch).
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